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text improvement
author
Bdale Garbee
<bdale@gag.com>
Tue, 23 Feb 2021 04:27:43 +0000
(21:27 -0700)
committer
Bdale Garbee
<bdale@gag.com>
Tue, 23 Feb 2021 04:27:43 +0000
(21:27 -0700)
rockets/airframes/MehGaNuke/index.mdwn
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diff --git
a/rockets/airframes/MehGaNuke/index.mdwn
b/rockets/airframes/MehGaNuke/index.mdwn
index 84131923537f9b5906fcce5a1bcf84e61b9e8020..141ac57379f58b5869df944fd5f3445fdd60fae1 100644
(file)
--- a/
rockets/airframes/MehGaNuke/index.mdwn
+++ b/
rockets/airframes/MehGaNuke/index.mdwn
@@
-136,8
+136,7
@@
on the main deployment bag. For this rebuild, 3 ribs will run the airframe
length between the 12" airframe and a concentric full-length 8" deployment
bay, with centering rings on each end. One sector of the rings will be
vented to allow apogee ejection gasses to flow from the charge cups on the
length between the 12" airframe and a concentric full-length 8" deployment
bay, with centering rings on each end. One sector of the rings will be
vented to allow apogee ejection gasses to flow from the charge cups on the
-leading edge of the fin can to push the nose off without push up on the
-main in its deployment bag.
+leading edge of the fin can to the nose, bypassing the main chute bay.
## Design / Simulation File
## Design / Simulation File