X-Git-Url: https://git.gag.com/?p=web%2Fgag.com;a=blobdiff_plain;f=rockets%2Fresearch%2F2017-test-12.mdwn;h=ba35937b2a8ca188c6a2447bb508b3dd7294d3c2;hp=81f314f18a6e8fb525b1a1372c2888895686c12e;hb=2045150506d8f63d150c97bba4a407b3b97546b4;hpb=3e16c14fa8347986b349ee98b7705a5ab6368e85 diff --git a/rockets/research/2017-test-12.mdwn b/rockets/research/2017-test-12.mdwn index 81f314f..ba35937 100755 --- a/rockets/research/2017-test-12.mdwn +++ b/rockets/research/2017-test-12.mdwn @@ -9,24 +9,32 @@ ring plus 0.25" inside liner, with two o-rings, one pushing against liner. Liner 23.125" long with about 22.25" available for fuel load. -Had to trim grains to fit. Four just required squaring up the ends and -trimming excess casting tube away. Fifth one was cut in miter box with saw. +Simulation says this is a 57% L-1366 with 3804 Ns total impulse, 797 psi max, +76% volume loading, and about 2.6 seconds burn time. -O-rings made forward closure a *very* snug fit. + +
CTI mod Sorbitol
Rating:57% L-1366Max Pressure:5.5 MPa
Total Impulse:3804 NsSpecific Impulse:131 s
Max Thrust:1706 NVolume Loading:76%
Average Thrust:1366 NFuel Mass:2958 g
null
+

Neglected to re-weigh grains after trimming and before epoxying into the -liner. +liner. These were the pre-trim masses: -* Grain , g gross, g net, 4.5" long -* Grain , g gross, g net, 4.5" long -* Grain , g gross, g net, 4.5" long -* Grain , g gross, g net, 4.4375" long -* Grain , g gross, g net, 4" long +* Grain 2017-7-1, 590g gross, 574g net, trimmed to 4.5" long +* Grain 2017-7-2, 594g gross, 578g net, trimmed to 4.5" long +* Grain 2017-7-3, 592g gross, 576g net, trimmed to 4.5" long +* Grain 2017-7-4, 584g gross, 568g net, trimmed to 4.4375" long +* Grain 2017-7-5, 580g gross, 564g net, cut to 4" long -Total of g propellant, vs g simulated. +Total propellant load thus somewhat less than 2860g. ## Results ## -Flight data logged as ? sn ?, flight ?. +Had to trim grains to fit. Four just required squaring up the ends and +trimming excess casting tube away. Fifth one was cut in miter box with saw. + +O-rings made forward closure a *very* snug fit. + +Flight data logged as sn 3121, flight 3 on 2017-10-08. 8353 ft apogee, Mach 0.7, 3.4 sec boost. +