X-Git-Url: https://git.gag.com/?p=web%2Fgag.com;a=blobdiff_plain;f=rockets%2Fresearch%2F2017-batch-03.mdwn;h=096f6bfcb838d8eb7725603075b20d63ab00509f;hp=b390854c016cf0344da0774710ff89edcf37208a;hb=b741d1a32d9390b08a72bc388094a00713b576a3;hpb=c3209ea421e038c69530f8f7e085d842dc212eda diff --git a/rockets/research/2017-batch-03.mdwn b/rockets/research/2017-batch-03.mdwn index b390854..096f6bf 100755 --- a/rockets/research/2017-batch-03.mdwn +++ b/rockets/research/2017-batch-03.mdwn @@ -14,26 +14,38 @@ increased during melting to 300F indicated. These grains were cast on 31 May 2017. -Liner should be cut to 10.00" long for this 6-grain reload. +Simulation says: + + +
29mm 6-grain Erythritol #14
Rating:43% H-162Max Pressure:5.92 MPa (859 psi)
Total Impulse:216 NsSpecific Impulse:133 s
Max Thrust:206 NVolume Loading:70%
Average Thrust:162 NFuel Mass:165 g
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+ +

## Results ## -* Grain 1, ?g gross, ?g net -* Grain 2, ?g gross, ?g net -* Grain 3, ?g gross, ?g net -* Grain 4, ?g gross, ?g net -* Grain 5, ?g gross, ?g net -* Grain 6, ?g gross, ?g net +Average casting tube mass 1.13g. -With a 10.00" liner, 14/64" nozzle throat, buna-n o-rings, simulation says -this makes a 37% H-156, 208 Ns, with about a 1.2 sec burn. +Coring rods extracted easily, new hickory tube caps came off without too +much effort. Slight cleanup at the top of each grain since propellant always +seems to fillet around the coring rod. Grain average fill levels looks pretty +good, with on the order of 1mm space at the top as expected. - -
29mm 6-grain Erythritol #14
Rating:43% H-162Max Pressure:859 psi
Total Impulse:48.5 lbf·sSpecific Impulse:133 s
Max Thrust:46.4 lbfVolume Loading:70%
Average Thrust:36.4 lbfFuel Mass:5.82 oz
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- +* Grain 1, 26.57g gross, 25.44g net +* Grain 2, 26.63g gross, 25.50g net +* Grain 3, 26.65g gross, 25.52g net +* Grain 4, 26.01g gross, 24.88g net (visible undefill) +* Grain 5, 26.51g gross, 25.38g net +* Grain 6, 26.75g gross, 25.62g net - -
29mm 6-grain Erythritol #14
Rating:43% H-162Max Pressure:5.92 MPa
Total Impulse:216 NsSpecific Impulse:133 s
Max Thrust:206 NVolume Loading:70%
Average Thrust:162 NFuel Mass:165 g
null
- -

+Total of 152.34g propellant, vs 159g simulated. + +Note that after casting grains and cutting a liner to 10.0", I realized I'd +mis-measured the case, and we actually had 10.4" of liner/propellant length +to play with! Fix this for the next time we make grains... For now, we'll +fly these grains in a correct length liner and live with the fact that we +could have put another 0.4" of propellant in the case! That'd be another +13 Ns according to the simulator... + +With a 10.40" liner, 14/64" nozzle throat, buna-n o-rings, simulation says +this reload will be a 37% H-155, 208 Ns, with about a 1.2 sec burn.