X-Git-Url: https://git.gag.com/?p=web%2Fgag.com;a=blobdiff_plain;f=rockets%2Fairframes%2FMehGaNuke%2Findex.mdwn;h=84131923537f9b5906fcce5a1bcf84e61b9e8020;hp=d79cb381879a73c2c7351cfd51dbb1d46c6fa07d;hb=d64500481ff811dd3dc3f4cd218136b76faf8671;hpb=b60145e545f2b6b36d7a88591a3f961adf14ccfc diff --git a/rockets/airframes/MehGaNuke/index.mdwn b/rockets/airframes/MehGaNuke/index.mdwn index d79cb38..8413192 100644 --- a/rockets/airframes/MehGaNuke/index.mdwn +++ b/rockets/airframes/MehGaNuke/index.mdwn @@ -110,9 +110,39 @@ The airframe is configured with two 1515-sized rail buttons, and is really only considered safe to launch from Terry Lee's launch trailer with 20 feet of very stiff 1515 rail. +### Revisions for Version 2 ### + +Because the main airframe zippered somewhat on the first flight, and the +ARRD released at apogee, rather than just repairing the existing airframe +tube, we're going to build a replacement. + +To increase stability, the main airframe tube length will be extended from +the original 4.5 feet to approximately 8 feet. The expected increase +in stability should allow a reduction in nose weight, increasing +safety. It should also make recovery system loading less arduous on the +rail. Of +course, this means the rocket will be closer to the length of an upscaled +Nuke Pro Maxx rather than the original Lil Nuke. + +For main deployment, the ARRD is being replaced with a +[Tender Descender L3](https://tinderrocketry.com/l13-tender-descender-tether), +which has the advantage that the release mechanism is orthogonal to the +axis of flight. That seems important when the airframe is this heavy and +apogee occurs at a non-nominal velocity, as in the first flight. + +The original build had internal 1x2 ribs and a baffle yielding a "D" shaped +main bay with the apogee charge gasses going up the channel without pushing +on the main deployment bag. For this rebuild, 3 ribs will run the airframe +length between the 12" airframe and a concentric full-length 8" deployment +bay, with centering rings on each end. One sector of the rings will be +vented to allow apogee ejection gasses to flow from the charge cups on the +leading edge of the fin can to push the nose off without push up on the +main in its deployment bag. + ## Design / Simulation File -[mehganuke.ork](/rockets/airframes/MehGaNuke/mehganuke.ork) +Original [mehganuke.ork](/rockets/airframes/MehGaNuke/mehganuke.ork) +Revised [mehganuke-v2.ork](/rockets/airframes/MehGaNuke/mehganuke-v2.ork) ## Construction Log @@ -183,16 +213,15 @@ deployment bag was not recovered. After studying the zipper and thinking about the main deployment sequence, several changes will be made before the next flight: - - The main airframe tube will be replaced with a tube that's a bit - longer (for greater stability), and has an internal 7.5-8" diameter - tube instead of the flat baffle to ease main chute deployment. + - The main airframe tube will be replaced with a tube that's a bit longer + (for greater stability), and has an internal 7.5-8" diameter tube instead + of the flat baffle to ease main chute deployment. - - Switch from the ARRD to the largest [Tender Descender](http://www.tinderrocketry.com/l13-tender-descender-tether) for main deployment + - Switch from the ARRD to the largest [Tender Descender](http://www.tinderrocketry.com/l13-tender-descender-tether) for main deployment. - - Add a TeleGPS to the nose assembly so it can be tracked - independently, and let it come down under the 2 existing 5-foot - chutes. Add a third 5-foot chute to be a dedicated pilot for the - 28-foot main chute. + - Add a TeleGPS to the nose assembly so it can be tracked independently, and let + it come down by itself under the 2 existing 5-foot chutes. Add a third 5-foot + chute to be a dedicated pilot for the 28-foot main chute. These changes should reduce the chance of another zipper, and reduce the amount of strap we need to stuff into the bay.